Well I have several days worth of work to write up so this is going to be a long post with a lot of images so please allow time for them to load in.
I’ll start with some background info about the bike, it was imported from japan in 2002 and is a 1997 model with 13.8k km about 8,600 miles. As far as I’m aware it was bought in either June 2005 or March 2006 and then was partly stripped down and the rear subframe was bent so it has a new frame. It was then partly rebuilt to the stage that I bought it from as the birth of twins got in the way and the bike was put on the way side. So this is where I pick up the story and Andy (will be following the story on this thread so hi =D )
On Saturday we went and got the bike in the usual way (shut up
@wornsprokets) bike one side and the 3 boxes of parts on the other.
Once home I started some uhh starting point photo.
I decided to plug the holes at the intake and gave it a little bit of a light wash with a spray can and my fingers as a brush/cloth because I was too lazy to get/find one.
I then after doing that decided to see if the engine would turn over. So I tried to remove the (carn’t remember its name) and it wouldn’t budge. So with a bit of persuasion (heat) it then cracked it finally came off. I then tried to turn the engine over and…thankfully the engine wasn’t seized and turned over nicely and this was a massive relief for me.
I gave the manifold a quick spray with TFR and that was it really. It'll get its own turn another day as it isn't a priority at the moment.
I then moved things swiftly inside and fitted the switch gears, clutch cable and the front master cylinder. I also tried to find how the airbox mounted and this took a lot longer than what it should have. Oh and I removed the rear cowl and cracked a lug on it but in my feeble defence it had already been broken once... oops.
After trying all 3 sets of carbs it was as always 3
rd time lucky and the last set I tired/remembered about was the best fit.
I added engine oil and it seemed to take a lot more than what I expected, I’ve also just realised as I’m typing this that I didn’t change the oil filter… come to think about it I don’t even know where the oil filter goes so I’ll have to look that up.
I then added the throttle cables and I thought I’d start on the back end... no innuendos please.
This is the wiring the came from the rear indicators into the looms, bare wire and perished rubber insulation.
So with a couple of new connectors and crimpers and a tactical and trusty Stanley knife blade everything was sorted and was working well.
I attached the carbs as far as I could get them and attempted to add some petrol into then attempted to start it up and it fired… I saw a flame from cylinder 2 come out of the manifold port and smoke came out the back of the carb… oops. So I knew at this point that the ht leads are in the wrong order. After trying to find out what order they went in I got them in the right order and she sparked into life… briefly. With that is was about 8pm and I went in happy.
So this is the end of what I think is day one.
So I guess this is uhh.. day two, so onwards weeeeeeeeee…..
Me and my mum set off for Wigan for a cb400sf nc31 (hear me out with this, ok?) for spares as mine needs a new loom ect and my mums car blew up just 25miles away from home. So after 3 HOURS I was back at home and could start work once again on the bandit.
I rummaged through some boxed and found the callipers, and it didn’t look good, the dust seal was hanging out of one of them, the pistons fully stuck and the pads falling apart with a touch of my finger. I then realised this was a spare so I removed the rubber standard hoses and fitted the braided hoses only to the master cylinder.
I filled the res with brake fluid and started pumping away and the lever wouldn’t pull back toward the bar then **crack** and it started moving. The lever would pull back to the bar and then would only move back so far so I decided to leave it overnight and see if the brake fluid would change anything since it has been dry for so long. I then removed the lever and coated everything in lm2 grease and everything works smoothly as it should.
I decided to do a test fit of the airbox so I unplugged a few wires to get it in without catching anything.
So I moved on from this and decided to attempt to start the bike once again. And it didn’t start I tried and tried different amounts of choke but it just wasn’t having it. After trying various things I decided to check the spark, no spark… eek but it was working yesterday. I must have spent 2-3hours on this. After checking every connection on the bike I decided the only thing I changed was the air box so I removed it and there was a 2 pin wire that was unplugged that was hiding along the underside of the frame plugged it in and tried again and she started. Called it a night and went to bed.
Last edited by Jameshambleton on Tue 25 Oct 2016, 9:12 am; edited 1 time in total